Hello everyone!
I built a quad and it was working ok, then two days ago I just updated OpenTX on my Taranis X7 Q's receiver from version 2.3.9 to 2.3.10. I have a fc Mateksys F722-SE programmed with Betaflight. But I got a little issue that got me stuck and I hope you could give me a direction....
After updated OpenTX's firmware , I checked AETR1234 protocol was correctly settled on the F722-SE and the order of channels into the taranis and the order is the same as like as it is settled on the fc.
To check everything I did:
- from Betaflight's motor test I check motors are working as individuals as all together;
- from Betaflight's Receiver I check throttle stick and I see the progress bar increasing/decreasing depending between -987 and +987 on what I want to do but I see also blue light on the fc blinking up so I go back to Motor Test and I try to arm the quad but in fact I see throttle doesn't rise motors up at least at minimum and I see the blue led blinking up.
I detached cable and I tried to gas motors from receiver and they doesn't rise up.
Considering channels are OK and before upgrade firmware it was ok (I did a backup of settings in Open Companion and then re-settled back after firmware update so it should be as like as it was before update), I am here asking all you if are there any differences between opentx 2.3.9 and 2.3.10 that would have messed throttle up? Or would be something else?...
Attached here the dump from Betaflight so maybe could be useful to give me a possible direction....
Thank you all !!!!
Cheers!
Jadawin
I built a quad and it was working ok, then two days ago I just updated OpenTX on my Taranis X7 Q's receiver from version 2.3.9 to 2.3.10. I have a fc Mateksys F722-SE programmed with Betaflight. But I got a little issue that got me stuck and I hope you could give me a direction....
After updated OpenTX's firmware , I checked AETR1234 protocol was correctly settled on the F722-SE and the order of channels into the taranis and the order is the same as like as it is settled on the fc.
To check everything I did:
- from Betaflight's motor test I check motors are working as individuals as all together;
- from Betaflight's Receiver I check throttle stick and I see the progress bar increasing/decreasing depending between -987 and +987 on what I want to do but I see also blue light on the fc blinking up so I go back to Motor Test and I try to arm the quad but in fact I see throttle doesn't rise motors up at least at minimum and I see the blue led blinking up.
I detached cable and I tried to gas motors from receiver and they doesn't rise up.
Considering channels are OK and before upgrade firmware it was ok (I did a backup of settings in Open Companion and then re-settled back after firmware update so it should be as like as it was before update), I am here asking all you if are there any differences between opentx 2.3.9 and 2.3.10 that would have messed throttle up? Or would be something else?...
Attached here the dump from Betaflight so maybe could be useful to give me a possible direction....
Thank you all !!!!
Cheers!
Jadawin
Attachments
Last edited: